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As I mentioned before, the car experienced significant
detonation at around 4300 RPM's. In addition to the fuel problem I believe there was
insufficient air flow through the intercooler. |
Here you can see the car being run on the chassis dyno.
You can also partially see the custom 3" exhaust. |
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Here is another picture of the car being prepared far a run.
You can see the Spearco Intercooler under the car. |
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